I’m working on a friends 2013 Avalanche left rear wheel arch rust out. The last coat of intercoat clear had a very bad reaction and approximately 50% of the panel checked. ( I kept the repair area very small- within 2” of wheel opening). The truck is in my paint booth with the windows blacked out to eliminate UV issues. Slow reducer was used in intercoat clear and base coat. My process to date:
1. Cut out rust and welded in repair sections around the wheel arch, approximately 1/3 of the circumference.
2. 2 coats unreduced SPI epoxy primer to all sanded bare metal (80 grit).
3. Polyester filler applied and sanded to 180 grit.
4. 2 coats unreduced epoxy primer to repair area.
5. Block sanded epoxy to 320 grit.
6. Sanded entire quarter panel to 800 grit to prepare for blend and new clear.
7. 1 coat 25% reduced epoxy sealer to repair area including slightly into sanded OEM. Blocked with 320 grit.
8. Final coat of 25% reduced sealer over repair to cover burn thru’s.
9. 1 coat of intercoat over entire quarter panel.
10. 3 days later, Denibbed and painted 1 additional coat of intercoat clear as a blending bed. Waited 1.5 hours to flash.
11. Laid down 2 coats of Sherwin Williams Ultra 7000 base coat with Sherwin Williams activator. Waiting 1 hour between coats.
12. Extended blend with 50% basecoat/50 intercoat. Each component was mixed 1:1 with their matching slow reducer. Both activated with their respective hardeners. Waiting 1 hour between coats.
13. One final coat intercoat clear to cap off metallics. Everything looked great. See photo.
14. 20 hours later, Found a small sag in basecoat and sanded out. (2” x 4”). Sprayed sanded area with basecoat using an air brush. Let flash.
So far everything looked fine, but bad things were about to happen.
15. 1 coat of intercoat over entire panel and was planning on clearing tomorrow. About 50% of panel immediately checked. See photos.
I’m at a loss where to go from here because I can’t figure out what the issue was that caused the reaction. I used this same process on my 1973 Mustang last year after discussing it with Barry and all went well. See photos. Any help figuring out what happened and the process to recover will be appreciated.
Thanks
Kevin
1. Cut out rust and welded in repair sections around the wheel arch, approximately 1/3 of the circumference.
2. 2 coats unreduced SPI epoxy primer to all sanded bare metal (80 grit).
3. Polyester filler applied and sanded to 180 grit.
4. 2 coats unreduced epoxy primer to repair area.
5. Block sanded epoxy to 320 grit.
6. Sanded entire quarter panel to 800 grit to prepare for blend and new clear.
7. 1 coat 25% reduced epoxy sealer to repair area including slightly into sanded OEM. Blocked with 320 grit.
8. Final coat of 25% reduced sealer over repair to cover burn thru’s.
9. 1 coat of intercoat over entire quarter panel.
10. 3 days later, Denibbed and painted 1 additional coat of intercoat clear as a blending bed. Waited 1.5 hours to flash.
11. Laid down 2 coats of Sherwin Williams Ultra 7000 base coat with Sherwin Williams activator. Waiting 1 hour between coats.
12. Extended blend with 50% basecoat/50 intercoat. Each component was mixed 1:1 with their matching slow reducer. Both activated with their respective hardeners. Waiting 1 hour between coats.
13. One final coat intercoat clear to cap off metallics. Everything looked great. See photo.
14. 20 hours later, Found a small sag in basecoat and sanded out. (2” x 4”). Sprayed sanded area with basecoat using an air brush. Let flash.
So far everything looked fine, but bad things were about to happen.
15. 1 coat of intercoat over entire panel and was planning on clearing tomorrow. About 50% of panel immediately checked. See photos.
I’m at a loss where to go from here because I can’t figure out what the issue was that caused the reaction. I used this same process on my 1973 Mustang last year after discussing it with Barry and all went well. See photos. Any help figuring out what happened and the process to recover will be appreciated.
Thanks
Kevin